PARR PAINTS
WASTE WATER ELIMINATION

Parr Paints solved its waste water problem by optimising cleaning processes and reusing the collected wash water in the next batch of product. The purchase cost ($800) of an off the shelf high pressure wash unit was more than offset by the $3000 pa savings in waste disposal and improved labour efficiency.

Background

Parr Paints Pty. Ltd. (Parr Paints) is a small family owned business that manufactures paints and textile coatings (latex adhesive). The company was started in 1971 and currently employs eight people.

Water based house paint accounts for about 80% of production, while solvent based paint accounts for the remaining 20%. The main water based paint is white acrylic suitable for tinting at the point of retail sale. Coloured acrylic paints (browns, reds and blacks) are also produced.

The Process

Waste water is generated from the clean out of the new blending tanks after each batch. The main types of waste water are:

The wash water from coloured acrylic paints and the latex was stored in 205 litre drums and spare vats pending pick up by a waste disposal company.

Cleaning of the latex blending tank was done using a low (mains) pressure hose and generated approximately 200 litres of wash water for each 800 litre batch. Approximately 800 litres of latex wash water was generated per month.

The company had made attempts to re-use the wash water in the next batch, but found that the ammonia and latex in the wash water caused the thickener to form lumps and impacted on product quality

ADD SET VOLUME WATER
ADD DISPERSANT/BIOCIDE
ADD STABILISER
ADD THICKENER
ADD FINAL VOLUME
WITH WATER
ADD LATEX
pH ADJUSTMENT WITH AMMONIA

Paint Pigment Ball Mill

Cleaner Production Initiative

The cleaner production initiative implemented by Parr Paints appears very simple in hindsight - changing the tank washing process to a high pressure system which has reduced wash water generation by 75%. More importantly this has allowed reuse of the latex wash water as make up water for the next latex batch, thereby eliminating a complete waste stream.

Parr Paints had previously focused on trying to treat the latex wash water so that it could be reused. However the wash water always "went off" before it was treated to a degree that would allow reuse.

An examination of the latex tank cleaning operation indicated that the use of a nozzle on a mains pressure hose was relatively ineffective. Because of this the operator also had to scrape down latex adhering to the tank walls.

Parr Paints decided to optimise the cleaning process first and then look at the process chemistry. Optimising the cleaning process by changing to an "off the shelf" low volume/high pressure cleaning unit reduced cleaning water requirements from 200 litres to approximately 40-50 litres. It was then found that this wash water could be totally reused in the next batch without any adverse impacts on product quality.

Advantages of The Process

The main advantage has been the elimination of the major source of waste water and the associated cost savings. The high pressure system has also decreased the time required for cleaning.

The direct cost savings are summarised in the following table:

Cost of High Pressure Unit

$800

Savings in Waste Disposal

$3,000 pa

Pay Back

1.7 months

 

Cleaner Production Incentive

There were a number of incentives for Parr Paints to address its waste water problem;

Latex Blending Tank

Barriers

The most significant barrier was concerns about the latex chemistry and the effect that the reuse of wash water would have on product quality. The thickener used in the latex is activated by ammonia and it was found that the residual ammonia in the wash water would form lumps when initial attempts were made to reuse it. Although the product was filtered to remove these lumps there was an adverse impact on product quality.

After consideration of the blending process it was realised that there was an opportunity to reduce the volume of wash water and use all of this as top up water for the next batch. As the top up water was added after the thickener the problem of lumping was overcome.

Involving the operator in the identification of the opportunity to reduce wash water was a key success factor.

Contact

Mr Howard Parr
Parr Paints Pty. Ltd.
38 Strong Avenue
Thomastown Vic 3074
Ph: 03-9460 7166
Fax: 03-9462 2636

Case Study Prepared By:
ACCP June 1998

Parr Paints received assistance under the Victorian Environment Protection Authority’s Cleaner Production Partnership Program for the reuse of latex wash water.