INTERNATIONAL CLEANER PRODUCTION INFORMATION CLEARINGHOUSE

CASE STUDY #24 1. Headline: Reducing heat loss in lead oxide unit 2. Background: In March 1993, the Energy and Environment Branch of the United Nations Industrial Development Organization (UNIDO), in close cooperation with the National Productivity Council (NPC) and several other industrial organizations in India, initiated a cleaner production demonstration project targeting small scale industries (SSIs) in India. The project DESIRE (Demonstration in Small Industries for Reducing wastE) began in March 1993. Its objectives included: - the demonstration of cleaner production opportunities and benefits to small-scale industries in India - the development of a systematic method for cleaner production - the identification of obstacles and incentives for cleaner production - the formulation of cleaner production policies. Three sectors: - agro-based pulp and paper production - textile dyeing and printing - pesticides formulation were targeted for demonstration projects, as they are sources of significant pollution and are primarily made up of SSIs. Four to six companies in each of the sectors have participated as demonstration units in the project. Although final results are awaited on DESIRE, preliminary data from the participating companies show economic and environmental improvements. A lead oxide unit, employing a pot type electrical furnace, manufactures one ton of lead oxide per day. A waste minimization audit at Sagar Surgicals Private Ltd found that the radiation heat losses from the side walls in the electric furnace was about 1600 KCals/m2 hour, and from the top, 2400 KCal/m2 hour. Due to there losses, the temperature inside the furnace was not adequate for obtaining the desired yield and quality of lead oxide. Additionally, fuel and power consumption and batch process time were high, and the furnace life was reduced due to overheating of the shell. The lead oxide unit at Sagar Surgicals employs a pot type electrical furnace, and manufactures one ton of lead oxide per day. 3. Cleaner Production Principle: Process modification 4. Description of Cleaner Production Application: The cleaner production applications mainly centered around process modifications. The furnace design was modified and better heat insulating material was used to reduce heat loss. Enabling technology: The existing insulation of fire bricks was replaced by better insulating materials of optimum thickness and sequence. A ceramic fibre module was added to the top of the furnace, and ceramic fibre blankets and insulating bricks were added to both the side walls and the top. 5. Economics: Savings US $/year Fuel consumption 6 600 Power consumption 3 300 Yield improvement 19 800 Capacity improvement 9 900 Total 39 600 US $/year Capital investment 10 000 Annual operating costs 5 000 Net annual savings 34 600 Payback period <3 months 6. Advantages: - Specific fuel consumption has been reduced from 80 to 40 liters/batch. - Specific power consumption has been reduced from 500 to 400KWh/batch. - The cycle time has decreased to 16 hours, from around 20-22 hours. - The furnace temperature has increased by 70C to 400C. - The percentage of lead oxide in the product has increased by around 3% to 31-33%. - The estimated increase in the life of the furnace is 4.5 years, from six months to five years. 7. Constraints: N/A 8. Contacts:Mr A.K. Asthana Director (Energy Conservation) National Productivity Council Swaroop Nagar Kanpur 208020 India Tel: +91 512 255635 Fax: +91 842 43634 Mr Shisher Kumra, Assistant Director Mr Rajeev Wadhwa, Deputy Director National Productivity Council 5-6 Institutional Areas Lodi Road New Delhi 110 003 India Tel: +91 11 461 1243 Fax: +91 11 461 5002 Mr Gudan Sagar Surgicals Private Ltd Panki, Industrial Estate Site 2 Panki, Kanpur 208020 India 9. Keywords:India, metal, lead oxyde, lead, process modification, insulation, DESIRE, energy saving, furnace 10. Reviewer comments: This case study was originally published in the UNEP IE document "Cleaner Production Worldwide", Volume II. In the process of preparing the document the case study underwent a technical review.